Extracted from The Fort Scott Tribune (Fort Scott, KS)
Brakes bad on bus in Arkansas crash
JASPER, Ark. (AP) -- A bus loaded with sightseers apparently was not
operating with full braking power and may have had some transmission
trouble when it left a winding Arksansas highway and plunged down a ravine,
killing 20 people, investigators says.
In addition, driver James Jefferson Thigpen, credited by some authorities
with doing all he could to save the lives of passengers, may have been
suffering from heart trouble and low blood sugar when his bus crashed
last week, according to a preliminary report by federal investigators.
``It appears as though the brake system on the bus was not 100 percent
operational,'' Claude Harris, one of the National Transportation Safety Board
investigators, said Monday.
Investigators said the bus was operating with 70 percent braking
power -- not enough to stop it -- at the time of the Thursday crash, the worst
in Arkansas history.
Twenty people were killed and 13 injured when the Central Texas
Buslines bus went out of control on a mountain road and plunged 50 feet
down a steep ravine. Officials said last week it appeared the 60-year-old
Thigpen, of Lancaster, Texas, had tried to use the ravine as a braking
mechanism in order to save the lives of his passengers, who were on a
sight-seeing tour from the Dallas area.
``There were physical problems with the driver, hypoglycemia and possibly
heart problems,'' said Tom Calderwood, head of the NTSB team, in
revealing the results of a preliminary autopsy report.
Hypoglycemia is a medical condition described as an abnormally low
concentration of sugar in the blood. The autopsy was done by state Medical
Examiner Dr. Fahmy Malak of Little Rock and Calderwood said Malak
would release details of the report later this week.
Investigators also said the bus had only ``70 percent effective braking''
power, as well as apparent problems with the transmission.
``Two air chambers which operate the brakes on two different wheels
appeared to be malfunctioning,'' Harris said. ``One additional drive
wheel appeared to have had a leaky grease seal on the bearings, which
would have made that brake system malfunction.
He said 70 percent power would not have been enough to stop the bus.
``We inspected all the linings on the brake system, and the linings
themselves were in acceptable shape,'' Harris said.
He said the driver also apparently had difficulty getting the bus into gear. He said a more detailed investigation of the apparent transmission problem
would begin today.
All other mechanical systems were operational, Harris said.
``The driver was described as being awake and alert and doing all he could
to maintain the vehicle on the highway,'' Calderwood said.
The passengers' testimony revealed the driver attempted to downshift when
the bus was already headed downhill.
``The first sign of trouble was the clashing gears and the lateral
acceleration of the bus, the pull of centrifugal force around sharp curves at a
high rate of speed,'' Calderwood said.
He said the investigation of the accident was about three-fourths completed
Monday.
Tuesday, June 10, 1980